Improving the Efficiency of Steam Turbine Rotor Manufacturing

DOI : 10.17577/IJERTV4IS041417

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Improving the Efficiency of Steam Turbine Rotor Manufacturing

Sharanakumar1

    1. ech student, Department of IEM M S Ramaiah Institute of Technology Bangalore, India

      Dr. Chethan Kumar C S2, S. Appaiap

      Professor2, 3, Department of IEM M S Ramaiah Institute of Technology

      Bangalore, India

      AbstractThe project was carried out at a reputed steam turbine rotor manufacturing unit, Bangalore. The product considered is steam turbine rotor used for generating power in sugar plant, it is a job order production. Previously, when this rotor was manufactured, the company was not able to supply the product to the customer at the promised time. The customer was not satisfied with this and demanded that the rotor be supplied in time. The cause for this was that the time required to manufacture this particular rotor was 7207 minutes which is quite high. The objective of this project is to reduce the cycle time of the steam turbine rotor manufacturing. The operations involved in steam turbine rotor manufacturing were noted and data was collected for each operation. The operations were classified into value added and non-value added activities and critical examination was applied to non-value added activities that took place on the CNC machine. The non-value added activities that were identified were approach checking, checking dimension values, inspection and chip cleaning. By the application of critical examination, the non-value added activity time was reduced from 1669 minutes to an estimated time of 635 minutes. Single Minute Exchange of Dies technique was applied for the three set up operations. The activities involved in the set up operations were divided into internal and external activities, reducing external and internal activities and then streamlining the internal activities. By doing so the set up operation time was reduced from 2280 minutes to an estimated time of 2140 minutes. By the application of critical examination and single minute exchange of dies technique, the cycle time to manufacture the steam turbine rotor is reduced from 7207 minutes to 6033 minutes. The estimated savings because of the cycle time reduction is found to be Rs. 1, 17,400/-.

      Keywords Cycle Time, Value Added Activities, Non Value Added Activities, SMED, Internal Activities, External Activities, Setup time.

      1. INTRODUCTION

        Method study is the technique of systematic recording and critical examination of existing and proposed ways of doing work and developing an easier and economical method [7] [8]. Method study is essentially used for finding better ways of doing work. It is a technique for cost reduction [9]. The philosophy of method study is that 'there is always a better way of doing a job' and the tools of method study are designed to systematically arrive at this better way of doing a job [12]. This procedure involves seven basic steps as follows [10]:

        1. Select the work to be studied.

        2. Record all facts about the method by direct observation.

        3. Examine the above facts critically.

        4. Develop the most efficient and economic method.

        5. Define the new method.

        6. Install the new method

        7. Maintain the new method by regular checking

        Single Minute Exchange of Die (SMED) is one of the many lean production methods for reducing waste in a manufacturing process [3]. It provides a rapid and efficient way of converting a manufacturing process from running the current product to running the next product [1]. This rapid changeover is key to reducing production lot sizes and thereby improving flow [11]. The phrase "single minute" does not mean that all changeovers and startups should take only one minute, but that they should take less than 10 minutes (in other words, "single-digit minute")[2]. Closely associated is a yet more difficult concept, One-Touch Exchange of Die, (OTED), which says changeovers can and should take less than 100 seconds.

      2. OBJECTIVES

        Productivity improvement by reducing the cycle time for Rotor manufacturing.

      3. METHODOLOGY

        • Selection of study to be carried out i.e., manufacturing of turbine rotor

        • First the entire processes during manufacturing of turbine rotor are recorded.

        • Identified Value added activities and Non Value added activities.

        • Total time taken for these above activities is recorded.

        • Critical Examination is done on Non value Added activities using Questioning technique

        • To reduce the setup time SMED technique is applied

        • Setup operations are recorded and analyzed.

        • Operations are divided into smaller elements and time taken for each element is noted.

        • Identify the internal and external element

        • Convert from internal steps into external steps

        • Reduce time consumed by the internal steps

        • Streamline the new process.

      4. EXISTING METHOD

        After recording the timings of all the operations the following observations were done.

        Setup time in min

        Machining time in min

        Non-value added time in min

        Total time in min

        2280

        3258

        1669

        7207

        Table 1: Components of Total time

        The non-value added activities time had the following components: approach checking, checking dimension values, inspection and chip cleaning.

        Approach checking time In min

        Inspection time In min

        Checking Dimension values In min

        Chip cleaning time In min

        378

        213

        408

        670

        Table 2: Components of Total time

        Present method time:

        Setup time = 2280 min

        Total Actual cutting time in min = 3258 min Total non value added time in min = 1669 min Total time = 7207 min

        Total time in hrs = 120 hr 6 min

      5. PROPOSED METHOD

        1. Critical Examination by Questioning Technique

          Develop For checking program dimensions values

          Before running the program, the operator has to check the dimension values with the data sheet. To avoid this, check list has been developed. By doing so we can eliminate or reduce this time. Before keying the programs to the machine, programmer has to cross check the dimension values in the program. Then inspector in the programming department has to recheck the program and it has to be approved by the programming department. Later it has to be sent to the production department for the process.

          1. Purpose What should be done?

            Provide the check list to reduce checking dimension values time.

          2. Place Where should it be done?

            It should be done at the programming department

          3. Sequence When should it be done?

            Soon after preparing the programs and before keying it into the machine

          4. Person Who should do it? Programming dept should do it.

          5. Means How should it be done?

            It should be done using process sheet.

            For approach checking

            This can be avoided by providing the checklist for the programming department. The programmer can cross check the program after developing the program. The same should be approved by the programming department. This reduces the operators time to check the program.

            1. Purpose What should be done?

              Provide the check list to reduce approach checking.

            2. Place Where should it be done?

              It should be done by the programming department

            3. Sequence When should it be done?

              After preparing the programs by the programmer

            4. Person Who should do it?

            Programming department should do it.

            Check list for Checking Dimension values and Tool approach checking during programming

            The checklist was prepared after discussion with the production engineer, supervisor, programmer and programming department head. This checklist has to be filled by the programmer after developing the program and get the program and the checklist checked and approved by the concerned authority.

            Project: Steam turbine rotor Frame: 012

            Drawing no: 002

            Table 3: Checklist

            Sl. No.

            Tool Description

            Tool path description

            Approach checking

            Checking Dimension Values

            Checked by

            1

            2

            3

            166

            Inspection time reduction Straight groove and coupling flange holes

            Inspection at the straight groove and coupling flange holes using slip gauges takes more time. To avoid this, inspection has to be done by using plug gauges. This would takes less time.

            Time reduction for Chip cleaning

            Chip cleaning activity is doing by manually and it is time consuming. To avoid this problem chip breaker has to be provided. By providing chip breaker, chip-cleaning time can be reduced.

            Estimated time savings after the application of Questioning Technique

            Sl.

            No.

            Setup Operations

            Internal Activity time

            in min

            External Activity time

            in min

            Remarks

            13

            Dis-engage both the weight support & engage of

            weight support in middle of component

            15

            14

            Machine the steady band areas. Select the depth of cut, cutting speed & feed rate

            20

            15

            Move the steadies in right positions & close them

            15

            16

            Machine 4 disc which are required to align component in this without chattering marks

            40

            17

            Adjust the steady rest by dial gauge in X-Y axis

            45

            18

            The tail stock end side disc can be aligned in X-axis

            by using a dial & adjustment screw provided on tailstock

            35

            19

            Work offset taken for probing

            70

            20

            Probe program altered outer diameter runned for X- Y alignment

            65

            21

            X-Y alignment probing

            85

            22

            Measure the same by measuring program and adjust the steady rest until to control the parameter

            120

            23

            Ensure the parameter readings once again that tolerance is within the limit(10-20 microns)

            45

            24

            check the raw part allowance related with the rough turning program

            70

            25

            After rough machining gross check the alignment of component by measuring program

            40

            26

            Disengage the both weight support and engage of weight support in the required position

            40

            27

            Remove the tail stock

            5

            28

            Probe program called and run

            55

            29

            X&Y Alignment done within 0.002micron

            80

            30

            Linear distance cross checked for disc 2-12

            65

            31

            Run out checked after alignment completion within 0.015micron

            110

            32

            Winding the rotor with belt

            10

            33

            Hook the rotor to the crane & check the belt is in balancing for lifting

            20

            34

            Disengage the steady rest Open the jaws and lift the rotor

            5

            35

            Open the jaws and lift the rotor

            40

            36

            Place the rotor on the rotor stand(without removing the belt with crane support)

            10

            External (Parallel to jaws

            removing)

            37

            Hard jaws removed and soft jaws mounted

            35

            External (Parallel to positionin g steady

            rest)

            38

            Cleaning

            15

            External (Parallel to placing

            rotor)

            39

            weight support steady rest position have to be found out so that the weight of the component uniformly distributed from the chuck till tail stock as per the position which has arrived from the

            following

            40

            40

            Check the jaws to be opened to enter the component Also check the Z-axis support length where the component rested which machining

            5

            External (Parallel to loading the componen

            t)

            1. first disc nearby chuck

            2. Second & third diameter nearby steady rest

            3. Fourth one nearby tail stock

            Table 4: Estimated cycle time for proposed method

            Setup time in min

            Actual cutting time

            in min

            Non-value added time

            in min

            Total time in min

            2280

            3258

            635

            6173

            Table 5: Non-value added time (Estimated) in proposed method

            Approach time In min

            Inspection time

            In min

            Checking D- values

            In min

            Chip cleaning time In min

            Nil

            104

            Nil

            531

        2. Single Minute Exchange of Dies technique

        The setup time in manufacturing of steam turbine rotor was

        more; to reduce this set up time we had applied Single Minute Exchange of Dies technique.

        Setup time reduction by SMED Technique

        Table No 6: Streamline the Internal and External activities

        35

        Sl.

        No.

        Setup Operations

        Internal Activity time

        in min

        External Activity time

        in min

        Remarks

        1

        cleaning of machine

        90

        2

        Removal of old jaws and fixing new jaws by manually

        External (Parallel to

        cleaning)

        3

        weight support steady rest position have to be found out so that the weight of the component uniformly distributed from the chuck till tail stock as per the position which has arrived from the

        following

        40

        External (Parallel to cleaning)

        4

        check the jaws to be opened to enter the component Also check the Z-axis support length

        where the component rested which machining

        5

        External (Parallel to

        cleaning)

        5

        winding the rotor with belt

        10

        External

        (Parallel to cleaning)

        6

        Hook the rotor to the crane & check the belt is in balancing for lifting

        20

        7

        Load the component in the machine & close the

        jaws softly so that the component is approximately in the center of the machine

        60

        8

        Remove the belt from rotor

        10

        9

        Engage the tail stock center. Ensure Z-axis butting

        5

        10

        Engage the weight support on steady rest 1& 2

        10

        11

        Check & correct the run out of component near by check. Tighten the hard jaws fully

        125

        12

        Once again check run out of the component on

        same diameter within same limit

        30

        Contd..

        Contd…

        Sl.

        No.

        Setup Operations

        Internal Activity time

        in min

        External Activity time

        in min

        Remarks

        41

        Load the component in the machine and close the jaws softly, so that the component is approximately

        in the center.

        60

        42

        Remove the belt from the rotor

        10

        43

        Engage the tail stock center. Ensure Z-axis is butting

        5

        44

        Engage the weight support on steady rest 1&2

        10

        45

        Check and correct the run out of the component nearby chuck. Tightened the hard jaws fully

        120

        46

        Once again check run out of component on same diameter within the same limit

        30

        47

        Steady holding on thrust collar outer diameter re- centering done

        80

        48

        Work offset taken for probing

        70

        49

        Probe program altered outer diameter run for X-Y axis alignment

        65

        50

        X-Y alignment probing

        85

        51

        Work offset taken and cross checked by measuring linear dimension

        70

        52

        C-axis done zero

        65

        TOTAL

        2195

        185

        Table No 7: Results

        Operations

        Present Method (time in min)

        Proposed Method (time in min)

        Savings (time in min)

        Non value added Activity

        Approach Checking

        378

        Nil

        378

        Inspection

        213

        104

        109

        Checking dimension values

        408

        Nil

        408

        Chip cleaning

        670

        531

        139

        Set up operations

        2280

        2140

        140

        Total

        3949

        2775

        1174

      6. RESULTS AND CONCLUSIONS

Critical examination was done for non-value added activities and the non-value added activities time was reduced from 1669 min to 635 min.

SMED Technique was applied to set up operations and set up time was reduced from 2280 min to 2140 min. Following table gives time taken for non-value added activities and set up operations for both present and proposed methods. Hence the cycle time was reduced from 7207 min to 6033 min.

  1. Results obtained

    Savings (estimated) after applying critical examination and single minute exchange of dies (SMED) technique.

    Cycle time (present method) = 7207 min Cycle time (proposed method) = 6033 Total saved time in min =1174

  2. Estimated savings (in terms of cost) to the company

    Loss to the company if machining operation is stopped per hour = Rs 6000

    Loss per min if machining operation is stopped = Rs 100 Total saved time in min (Estimated) = 1174

    Net savings per Rotor (Estimated) = 1174*100 Net savings per Rotor (Estimated) = Rs. 117400

    Most of the suggestions given for reducing the cycle time of this steam turbine rotor hold good for many of other types of rotor also. Hence, these suggestions can be implemented for other rotors and cycle time and cost can be reduced to a great extent.

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